Information From Previous Years


1.0 About the Solar Splash Race/Competition

The American Society of Mechanical Engineers (ASME) sponsored Solar Splash '94, which was held August 18-21, 1994 on Pewaukee Lake just west of Milwaukee, Wisconsin. The event was hosted by Marquette University and the Pewaukee Lake Yacht Club. Teams arrived during the day on August 18 to register and prepare for the weekend of racing. Qualifying and technical inspections were held on August 19. Qualifying consisted of each entry completing one lap of a course designed to test maneuverability as well as passing several safety tests, including static stability and driver egression. Times from the qualifying laps were then used to seed the entries for the sprint races held on August 20. Each sprint race consisted of running down a two hundred meter straight-away course starting from a stationary position. There were four rounds in all. The first round was used to seed the entries for the second round and to confirm the qualifying results. The second and third rounds were elimination rounds setting up a four boat final heat. The endurance races were held August 21 on a closed loop course around which participants piloted their craft for two hours. Participants were judged on the number of laps completed within the alloted time. There was a preliminary round held in the morning and a final round held in the afternoon.

Solar Splash '94 gained international recognition and attracted participants from all over the world. The participants were University of Michigan, Kanazawa Institute of Technology (Japan), Kobe University of Mercantile Marine(Japan), University of Puerto Rico, Marquette University, McNeese State University, University of South Carolina, Western New England College, University of Arkansas, and Grand Valley State University. The Solar Splash staff has already reported inquiries from over sixty potential entries for the 1995 Regatta.

2.0 Solar Splash '94 Results

The results from the 1994 Solar Splash Regatta were as follows:

Result Sprint Race Endurance Race
1st Place Kanazawa Institute of Technology Kanazawa Institute of Technology
2nd Place University of Arkansas University of Puerto Rico
3rd Place University of Michigan Kobe University of Mercantile Marine


University of Michigan highlights: 3rd Place Sprint; Mechanical Technical Achievement Award; DNF Endurance. The University of Michigan was unable to compete in the endurance race due to structural failure of a universal joint.

3.0 Team Development

The University of Michigan Solar/Electric Boat Team began to take shape in January 1994. The team is a derivative of another design team that had begun working on an entry for the Human Powered Submarine races that are held annually off of the coast of Florida. The team leaders of the original Human Powered Submarine Team received a fax from Marquette University inviting them to participate in Solar Splash '94. The Human Powered Submarine Team, while still in its infancy and short on personnel, was forced to make a decision. The decision was whether to proceed with the Human Powered Submarine, or to withdraw from that event and to enter Solar Splash '94. After lengthy discussions and a team vote, the decision was made to proceed with the solar/electric boat pro ject for several reasons. The most attractive aspect of the solar/electric boat project was that it was an engineering contest that eliminated the dependence on athletic prowess. Another attractive feature of the solar/electric boat project was that the technology developed would be more applicable to real world problems. Team members were also excited by the prospect that virtually anyone could pilot the boat. This was not true for a human powered submarine because only certified SCUBA divers are allowed t o pilot such a vehicle. These three factors proved to be enough to sway the team to enter the 1994 Solar Splash Regatta.

4.0 Design Direction

The team was late in entering the event and with only six months to design and construct a solar/electric boat, we decided to focus our efforts on the sprint race. Producing a boat that could win both the sprint and the endurance races would require more time and funds than were available. In addition, the University of Michigan has expertise in the area of planning hull design which we felt was unavailable to other teams. Concentrating on a planning sprint boat would also allow the team to test innovative ideas as in planning hull technology.

Trading viscous drag for pressure drag (i.e. reducing viscous drag and increasing pressure drag) is in general a positive trade with regard to increasing speed. Thus, increasing the ratio of pressure drag to viscous drag can produce an increase in speed for a given power requirement (i.e. net drag).Therefore, in order to get the highest speed out of a given power supplied, the objective becomes to reduce the wetted surface of the hull.

This reduction in wetted surface can be accomplished by decreasing the draft of the boat via dynamic lift. There are several types of watercraft that produce dynamic lift which include planing hulls, hydrofoil assisted hulls, and surface effect hulls. The use of a surface effect hull was ruled out early in the design process because it either requires a large amount of power at zero forward speed (i.e. air cushion vehicles), or it requires very high forward speeds (i.e. ramjet vehicles) in order to produce dynamic lift. Over the course of two hundred meters one can neither afford to expend power that does not result in forward speed nor expect to attain speeds high enough to achieve ramjet effects. Hydrofoil assisted hulls are often difficult to design and build. This is due to the difficulties associated with structurally supporting the hydrofoils, and the need for complex control surfaces. These factors, combined with the availability of planing hull technology at the University of Michigan led the team to design and construct a planing hull. In hindsight,this was an excellent decision because none of the three teams who designed their craft to use hydrofoils actually used them at Solar Splash '94. One team encountered structural problems with supporting their foils, and the underwater lake vegetation inhibited any team using underwater appendages.

The planing hull surface and propeller were designed using computer modeling tools developed at the University of Michigan in conjunction with Michigan Sea Grant and Vorus & Associates Incorporated. In order to investigate unproven concepts in planing hull technology, the team decided to attempt the design and construction of an inverted vee planing hull under the advisement of our faculty advisor Dr. William S. Vorus. It was theorized that the inverted vee would not only provide lateral stability in shallow draft conditions, but also provide added lift from the interaction of the internal jet heads and reduce the wetted surface by causing flow separation at the wing tips. In the process of making the decision to design and construct this planing hull, the team set two goals. The first goal was to get such an innovative concept to successfully plane given the maximum electrical energy available. The second goal was to attain a top speed of twenty miles per hour.

The decision to use a surface piercing propeller was driven by the shape of the transom and the desire to minimize appendage drag. With an inverted vee shape at the transom, it is difficult to support a fully submerged propeller without encountering increased appendage drag from subsurface structural members. In addition, a properly designed fully cavitating surface piercing propeller can take advantage of the aforementioned trade-off between viscous and pressure drag.

Appendage drag could be further reduced by not having submerged steering devices. The team therefore decided that maneuvering would be accomplished by shifting the pilot's lateral position. This would create a net turning moment due to a lateral displacement of both the center of gravity and the net drag vector.

5.0 Hull Design & Construction

5.1 Design
Computer simulation was used to determine an internal deadrise distribution over the running wetted length that would bring the hull lift to drag ratio to a predetermined level. Once the deadrise distribution was determined, the internal running wetted surface was modeled using the software package FastShip4.13. The rest of the hull surfaces were then designed to meet both hydrostatic displacement and functional requirements. With all of the surfaces modeled, offsets were taken from the hull sections and exported to AutoCAD to produce design drawings for lofting.

5.2 Construction
With funding from Trinity Marine Group the UMSEBT participated in and supervised construction of the hull at United States Marine, Incorporated. The male mold was fabricated with 3/4" plywood sections covered with 1/8" Lewan plywood. The composite hull was constructed by bonding a single skin of carbon fiber to each side of 1/2" Divinycell H60 foam core using Derakane 8084 vinylester resin as the bonding agent. Because of the inverted vee design, it was impossible to pull the hull in a single part from the male mold. Therefore,the decision was made to lay the foam core over the mold and then bond the external layer of carbon fiber to the core. The mold then had to be disassembled and removed from within the partially completed hull. With the internal surface of the foam core exposed, the internal layer of carbon fiber could be bonded in place. With the basic hull form complete, the hull was shipped back to the University of Michigan and structural members and motor supports were installed. The external surface was then finish-sanded, primed and painted.

6.0 Propeller Design & Fabrication

The propeller was custom designed using computer modeling software at the University of Michigan. The final design was for a five-bladed,twelve inch diameter, fully cavitating, surface piercing propeller that would be fifty percent submerged in the running condition. NuCon Marine Systems Corporation provided funding for and fabrication of the propeller from T6061-T6 aluminum using five-axis milling technology.

7.0 Propulsion System and Machinery

7.1 Motor Selection
Preliminary power requirements guided the search for four to ten horsepower motors. Initial race specifications required that the motors operate on a system voltage not to exceed twenty-four volts. Cost and high amperage requirements eliminated the use of brushless DC motors and narrowed the search to permanent magnet DC motors. Under advisement from Gabriel Marine, the team selected two Advanced DC A-89 series wound traction motors for their capability of handling the high current loads expected in the sprint race.

7.2 Thrust Vectoring
A surfacing propeller produces significant lateral forces because only half of the blades are submerged, and thus experience side forces in the running condition. This produces a turning moment acting on the hull. In order to eliminate this turning moment the net lateral force on the system must be zeroed. This can be achieved by laterally canting the shaft relative to the centerline of the hull to produce a zero net turning moment.

7.3 Adjustable External Shaft Support
Uncertainties exist in the prediction of propeller placement necessary for both zeroing the turning moment and achieving fifty percent propeller submergence in the running condition. Therefore both the horizontal and vertical position of the propeller had to be adjustable. These requirements lead to the design and fabrication of a propeller positioning system consisting of a universal joint and an external thrust bearing constrained by five adjustable tie-rods. The universal joint allowed the shaft to be canted without altering the position of the internal shaft and motors. The thrust bearing consisted of two Rulon flange bearings press fit into a stainless steel collar. The collar was fabricated at Brighton NC Machining and was held in place by the five adjustable tie-rods which transmitted the thrust from the thrust bearing to the hull. This in turn kept the thrust loads from reaching the universal joint.

7.4 Gearing
The two Advanced DC A-89 motors were connected to the shaft via two rollerchains and sprockets. The propeller was designed to operate at 1800 RPM in the running condition. The roller chain/sprocket combination was used to allow forgearing changes based on propeller RPM during trial runs. The design gear ratio was 3:1 (motor/shaft).

8.0 Electrical System

All teams were required to remove their solar arrays during the sprint event due to the short duration of the races. However, the Solar Splash '94 rules stipulated that all battery recharging must be accomplished with solar panels. Since we decided to focus the sprint race and had minimal resources, the team decided not to invest in the design and fabrication of a costly, high quality solar array. In lieu of such an extravagant system, we decided to purchase two off-the-shelf solar panels that would produce enough power to top off the batteries after each sprint race.

The batteries for all of the teams competing in Solar Splash '94 were donated by Johnson Controls. Two types of 12 VDC batteries were made available to the teams, one with an 81 amp-hour rating and the other with a 51 amp-hour rating. Both types of batterie s had a maximum discharge capacity of one thousand amperes.

Due to the high current loads in the high power system, 2/0 cable was used to minimize the power loss through the cables. The rules called for a high power battery disconnect in line with a separate high power motor disconnect. The motor disconnect consist ed of four high power contactors connected in parallel. To maximize power output for the sprint race, the control system simply consisted of a spring loaded on/off switch which engaged the contactors. However, for testing purposes and the endurance race a variable speed control was desired. This was accomplished by installing two DC motor controllers which were both operated from a single spring loaded potentiometer. Ford Motor Company financed the purchase of the motors, motor controllers, and associated electrical equipment from Electric Vehicles of America.

9.0 Operational Phases

9.1 Testing
In order to establish the boat as a safe and stable platform, it was towed behind a ski-boat to test planing stability and maneuvering prior to the installation of the motors and electrical system. Once the boat was deemed seaworthy, the motors were installed and fully operational sea trials commenced. After making several adjustments to the propeller position and removing part of the deck to reduce weight, the boat was not performing up to expectations. The team was unable to get the boat planing prior to departing for Solar Splash '94 and the top speed attained was under ten miles per hour.

9.2 Racing
It was felt that the propeller was not developing enough thrust at low speed and that lowering the propeller should develop enough increased thrust to get the boat up on plane. Despite further modifications to the propeller position,the boat's performance was not improved for race qualifying. However, it was established during qualifying that the boat was more than maneuverable enough under sufficient forward speed to complete the qualifying course and meet the minimum turning radius requirement of forty meters.

The team did not feel that the Vee-N-Verse's performance in the qualifying round would be competitive in the sprint event. The boat was not performing upto our design goal, which was to plane. For this reason the team decided to make two major changes in the propulsion system with hopes of increasing the performance. However, there would be no time to test the new configuration prior to the first heat in the sprint event, which made the team's decision a risky one. The first major alteration in the propulsion system was to replace our two 12 VDC 81 amp-hour batteries with three 12 VDC 51 amp-hour batteries. This alteration was approved by the race committee after another team was allowed to boost their system voltage to 96 volts by means of a DC-DC converter. The second major change to the propulsion system was to modify the sprockets on both the shaft and the motors to give the system a 1:1 gear ratio. This allowed the motors to operate at the design RPM on the new system voltage of 36 VDC with an increase in power. Despite these drastic adjustments the Vee-N-Verse was still not able to plane in the first round of the sprint competition.

Before the second round, which was to be the first elimination round, the team made one final adjustment to the propeller location by lowering it about two inches in an attempt to improve performance. The increased thrust at low speed due to this adjustment was enough to vault Vee-N-Verse up onto plane for the first time. This cut our elapsed time from seventy-four seconds in the first round to thirty-nine seconds in the second round. This improved time was good enough to place us in the semifinals where we ran the course in thirty-three seconds and advanced to the final round. In the final round the Vee-N-Verse repeated her semifinal time of thirty-three seconds which secured third place overall in the sprint competition for the UMSEBT.

Unfortunately, the Vee-N-Verse suffered mechanical failure of a universal joint during the sprint race finals. For fear of suffering irreparable damage to theboat and endangering the pilot's safety, the UMSEBT was forced to withdraw the Vee-N-Verse from the endurance competition. After a successful weekend of racing the UMSEBT returned to Ann Arbor, Michigan having earned the Mechanical Technical Achievement Award and Third Place overall in the Sprint Event ofSolar Splash '94.

9.3 Post Race Improvements
Although the Vee-N-Verse performed exceptionally well under the harsh conditions encountered at Solar Splash '94, it was felt that the boat's performance could still be improved. The team decided to attempt to reach the design speed of twenty miles per hour . The boat was refitted with a needle-bearing universal joint that would provide smoother operation, and taken back to North Lake for final testing. During this testing the Vee-N-Verse exceeded the design goal by attaining a top speed of twenty-one miles per hour and handling exceptionally well during rigorous maneuvering tests. The testing also allowed the three members of the team who designed and constructed the boat, James Criner, Greg Beers, and Bryan Johnson to each experience the thrill of piloting the Vee-N-Verse.

10.0 Future Improvements

The UMSEBT has compiled a list of potential improvements to the existing Vee-N-Verse. One of the simplest yet critical improvements is to realign the motors and internal shaft to reduce the angle on the universal joint. This will increase the torque bearing capacity of the universal joint and will reduce mechanical losses. Another important modification is to strip and refinish the exterior surface of the hull. Doing this under strict quality control will improve both the boat's appearance and reduce the weight associated with excess paint. Further reduction of the overall boat weight will allow the Vee-N-Verse to attain higher speeds and quicker acceleration. To achieve this the boat will undergo a weight reduction program which ranges from cutting limber holes in many of the outfitting components to removing any unnecessary structure. Reducing the overall weight by as little as ten pounds has been shown to have a significant impact on the boat's performance. A substantial improvement to the drive system will be to use timing belts to transmit power in lieu of the existing roller chains and sprockets. This will reduce mechanical losses associated with the gearing and lessen the vibrations in the system.

The electrical system needs to be completely revised to make better use of the energy available in the batteries. This should also reduce the amount of copper cable used in the existing electrical system which will in turn save weight. The team also plans to design, construct, and employ a high quality solar array for use in the 1995 Solar Splash. This is an expensive and time consuming activity that will require significant sponsorship. The goal is to develop an array which could provide enough power to al low the Vee-N-Verse to be competitive in the endurance event without drastic hull modifications. Also, the team will need to design and fabricate a second propeller for use in the endurance event. The existing surface piercing propeller, while providing excellent performance in the design condition, is not intended to operate at low speeds.

An eventual goal for Vee-N-Verse is to have a computer controlled propellerpositioning system. This system will move the propeller from an optimum position for accelerations from a standing start to an optimum position for the running condition. If this goal is not attainable for Solar Splash '95, the existing propeller positioning system still must be improved because it can be cumbersome to work with.

11.0 Conclusion

Throughout this discussion we have touched on the rationale behind most of the decisions and actions made by the UMSEBT during the course of the design and construction of Vee-N-Verse. While a complete discussion of the rational engineering used to produce Vee-N-Verse is beyond the scope of this discussion, the validation of such an approach is not. In section 4.0 Design Direction, it was stated that the team's goal for Vee-N-Verse was to successfully achieve a top planing speed of twenty miles per hour. After six months of hard work and generous sponsorship, the UMSEBT exceeded that goal by attaining a top planing speed of twenty-one miles per hour. With only six months to complete the project, the UMSEBT was not afforded the luxury of design iteration and testing. It is our contention that the success of this project was a direct result of the persistent use of rational engineering.

12.0 Acknowledgments

The University of Michigan Solar/Electric Boat Team would like to take this opportunity to recognize the following companies and individuals for their generous sponsorship. Without your support, our dream could never have become a reality.